American Airlines Flight 191
Template:Short description Template:For Template:Good article Template:Use mdy dates Template:Use American English Template:Infobox aircraft occurrence American Airlines Flight 191 was a regular scheduled domestic passenger flight from O'Hare International Airport in Chicago to Los Angeles International Airport. On the afternoon of May 25, 1979, the McDonnell Douglas DC-10 operating this flight was taking off from runway 32R at O'Hare International when its left engine detached from the wing, causing a loss of control. The aircraft crashed about Template:Convert from the end of runway 32R. All 271 occupants on board were killed on impact, along with two people on the ground. With a total of 273 fatalities, the disaster is the deadliest aviation accidentTemplate:Efn to have occurred in the United States.<ref name=wihiserg>Template:Cite news</ref><ref name=upiprp>Template:Cite news</ref><ref name=toncijc>Template:Cite news</ref>
The National Transportation Safety Board (NTSB) found that as the aircraft was beginning its takeoff rotation, engine number one (the left engine) separated from the left wing, flipping over the top of the wing and landing on the runway. As the engine separated from the aircraft, it severed hydraulic lines that lock the wing's leading-edge slats in place and damaged a Template:Convert section of the left wing's leading edge. Aerodynamic forces acting on the wing resulted in an uncommanded retraction of the outboard slats. As the aircraft began to climb, the damaged left wing produced far less lift than the right wing, which had its slats still deployed and its engine providing full takeoff thrust. The disrupted and unbalanced aerodynamics of the aircraft caused it to roll abruptly to the left until it was partially inverted, reaching a bank angle of 112°, before crashing in an open field by a trailer park near the end of the runway. The engine separation was attributed to damage to the pylon structure holding the engine to the wing, caused by improper maintenance procedures at American Airlines.<ref name=argtsblm>Template:Cite news</ref><ref name=mtcpro>Template:Cite news</ref><ref name=tobldap>Template:Cite news</ref>
Background
Aircraft
The aircraft involved was a McDonnell Douglas DC-10-10 registered as N110AA. At the time of the crash, it had logged just under 20,000 hours of flying time over seven years since it was delivered in 1972. The aircraft was powered by three General Electric CF6-6D engines.<ref>Template:Cite web</ref> A review of the aircraft's flight logs and maintenance records showed that no mechanical discrepancies were noted for the day before the accident. The logs for the previous flights that had occurred on the day of the accident had not been removed from the logbook, in violation of standard procedure, and were destroyed in the accident.<ref name="NTSB AAR-79-17 Final Report" />Template:Reference page
Flight crew
Captain Walter H. Lux (age 53) had been flying the DC-10 since its introduction eight years earlier. He had logged around 22,000 flying hours, of which about 3,000 were in a DC-10. He was also qualified to pilot seven other aircraft, including the DC-6, DC-7, and Boeing 727.<ref name="NTSB AAR-79-17 Final Report" />Template:Reference page First Officer James Dillard (age 49) and Flight Engineer Alfred Udovich (age 56) were also highly experienced. Dillard had accumulated about 9,275 flying hours, of which 1,080 were in a DC-10; Udovich had about 15,000 hours, of which 750 were in a DC-10.<ref name="AirDisaster">Template:Cite web</ref>
Accident
On the accident flight, during the takeoff rotation, the number-one engine and its pylon assembly separated from the left wing, ripping away a Template:Convert section of the leading edge with it. The combined unit flipped over the top of the wing and landed on the runway.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page Robert Graham, supervisor of maintenance for American Airlines, stated: Template:Blockquote
What was said in the cockpit in the 31 seconds leading up to the final impact is not known, as the cockpit voice recorder (CVR) lost power when the engine detached. The only crash-related audio collected by the recorder is a thumping noise (likely the sound of the engine separating), followed by the first officer exclaiming, "Damn!", at which point the recording ends. This may also explain why air traffic controllers were unsuccessful in their attempts to radio the crew and inform them that they had lost an engine. This loss of power did, however, prove useful in the investigation, serving as a marker of exactly what circuit in the DC-10's extensive electrical system had failed.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page

In addition, due to the loss of the engine, several related systems failed. The number-one hydraulic system, powered by the number-one engine failed, but continued to operate through motor pumps that mechanically connected it to hydraulic system three. Hydraulic system three was also damaged and began leaking fluid, but maintained pressure and operation until impact. Hydraulic system two was undamaged. The number-one electrical bus, the generator of which was attached to the number-one engine, failed as well, causing several electrical systems to go offline, most notably the captain's instruments, his stick shaker, and the slat disagreement sensors. A switch in the overhead panel would have allowed the captain to restore power to his instruments, but it was not used. The flight engineer might have reached the backup power switch (as part of an abnormal situation checklist, not as part of their takeoff emergency procedure) to restore electrical power to the number-one electrical bus. That would have worked only if electrical faults were no longer present in the number-one electrical system. To reach that backup power switch, the flight engineer would have had to rotate his seat, release his safety belt, and stand up. Regardless, the aircraft did not get any higher than Template:Convert above the ground and was in the air for only 31 seconds between the time the engine separated and the moment it crashed; there was insufficient time to perform such an action. In any event, the first officer was flying the airplane, and his instruments continued to function normally.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page

The aircraft climbed to about Template:Convert above ground level while spewing a white mist trail of fuel and hydraulic fluid from the left wing. The first officer followed the flight director and raised the nose to 14°, which reduced the airspeed from Template:Convert to the takeoff safety airspeed (V2) of Template:Convert, the speed at which the aircraft could safely climb after sustaining an engine failure.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
The engine separation severed the hydraulic fluid lines that controlled the leading-edge slats on the left wing and locked them in place, causing the outboard slats (immediately left of the number-one engine) to retract under air load. The retraction of the slats raised the stall speed of the left wing to about Template:Convert, Template:Convert higher than the prescribed takeoff safety airspeed (V2) of 153 knots. As a result, the left wing entered a full aerodynamic stall. With the left wing stalled, the aircraft began banking to the left, rolling over onto its side until it was partially inverted at a 112° bank angle with its right wing over its left wing.

Since the cockpit had been equipped with a closed-circuit television camera positioned behind the captain's shoulder and connected to view screens in the passenger cabin, the passengers may have witnessed these events from the viewpoint of the cockpit as the aircraft dove towards the ground.<ref>Template:Cite news</ref><ref>Template:Cite news</ref> Whether the camera's view was interrupted by the power loss from the number-one electrical bus is not known.<ref name=urldpld>Template:Cite news</ref> The aircraft eventually slammed into a field around Template:Convert from the end of the runway.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page Large sections of aircraft debris were hurled by the force of the impact into an adjacent trailer park, destroying five trailers and several cars. The DC-10 also crashed into an old storage hangar at the edge of the airport at the former site of Ravenswood Airport. The aircraft was destroyed by the impact force and ignition of a nearly full load of Template:Convert of fuel; no sizable components other than the engines and tail section remained.<ref>Template:Cite book</ref>
The crash site is a field located northwest of the intersection of Touhy Avenue (Illinois Route 72) and Mount Prospect Road on the border of the suburbs of Des Plaines and Mount Prospect, Illinois.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
Victims
In addition to the 271 people on board the aircraft, two employees at a repair garage near the impact site were killed, and two more were severely burned.<ref name="NTSB AAR-79-17 Final Report" />
Nationalities of the victims
| Nation | Passengers | Crew | Ground | Total |
|---|---|---|---|---|
| United States | 247 | 13 | 2 | 262 |
| Saudi Arabia | 4 | Template:N/a | Template:N/a | 4 |
| South Korea | 1 | Template:N/a | Template:N/a | 1 |
| Austria | 1 | Template:N/a | Template:N/a | 1 |
| Belgium | 1 | Template:N/a | Template:N/a | 1 |
| Netherlands | 4 | Template:N/a | Template:N/a | 4 |
| Total | 258 | 13 | 2 | 273<ref>Template:Cite news</ref> |
Passengers
Two of the victims in the crash of Flight 191 were:
- Itzhak Bentov, a Czechoslovakia-born Israeli–American biomedical inventor (the cardiac catheter) and New Age author (Stalking the Wild Pendulum and A Cosmic Book)<ref>Template:Cite news</ref>
- Leonard Stogel, music business producer/manager/promoter/executive for California Jam, California Jam II, Sweathog, The Cowsills, Sam the Sham, Tommy James and the Shondells, Redbone, Gentle Giant, and other musical groups. Stogel's parents had died in an accident in 1962 on American Airlines Flight 1 in New York City.<ref>Template:Cite news</ref><ref>Template:Cite news</ref>
Memorial
For 32 years, the victims had no permanent memorial. Funding was obtained for a memorial in 2009 through a two-year effort by the sixth-grade class of Decatur Classical School in Chicago.<ref>Template:Cite web</ref> The memorial, a Template:Convert concave wall with interlocking bricks displaying the names of the crash victims, was formally dedicated in a ceremony on October 15, 2011.<ref>Template:Cite news</ref> The memorial is located on the south shore of Lake Opeka, at Lake Park at the northwest corner of Lee and Touhy Avenues,<ref>Template:Cite web</ref> two miles east of the crash site. A remembrance ceremony was held at the memorial on May 25, 2019, the 40th anniversary of the accident.<ref>Template:Cite news</ref>
Thirty victims whose remains were never identified are buried at Green Hills Memorial Park in Rancho Palos Verdes, California.<ref>Template:Cite news</ref> The site of the crash was redeveloped around March 2021, and has been named the future site of an interchange for Interstate 90/Interstate 490.<ref>Template:Cite news</ref>
Investigation
The disaster and investigation received widespread media coverage. The impact on the public was increased by the dramatic effect of an amateur photo taken of the aircraft rolling that was published on the front page of the Chicago Tribune on the Sunday two days after the crash.<ref>Template:Cite web</ref>
Engine separation

Witnesses to the crash were in universal agreement that the aircraft had not struck any foreign objects on the runway. In addition, no pieces of the wing or other aircraft components were found along with the separated engine, other than its supporting pylon; this led investigators to conclude that nothing else had broken free from the airframe and struck the engine. Hence, the engine/pylon assembly separation could only have resulted from a structural failure. The cockpit instrument panels were damaged so badly that they did not provide any useful information.<ref name=vatz />
During the investigation, an examination of the pylon attachment points revealed some damage done to the wing's pylon mounting bracket that matched the bent shape of the pylon's rear attachment fitting. This meant that the pylon attachment fitting had struck the mounting bracket at some point. This was important evidence, as the only way the pylon fitting could strike the wing's mounting bracket in the observed manner was if the bolts that held the pylon to the wing had been removed, and the engine/pylon assembly was supported by something other than the aircraft itself. Therefore, investigators could now conclude that the observed damage to the rear pylon mount had been present before the crash occurred rather than being caused by it.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
The NTSB determined that the damage to the left-wing engine pylon had occurred during an earlier engine change at the American Airlines aircraft maintenance facility in Tulsa, Oklahoma, between March 29 and 30, 1979.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page On those dates, the aircraft had undergone routine service, during which the engine and pylon had been removed from the wing for inspection and maintenance. The removal procedure recommended by McDonnell-Douglas called for the engine to be detached from the pylon before detaching the pylon itself from the wing. However, American, as well as Continental Airlines and United Airlines, had developed a different procedure that saved about 200 working hours per aircraft and "more importantly from a safety standpoint, it would reduce the number of disconnects (of systems such as hydraulic and fuel lines, electrical cables, and wiring) from 79 to 27."<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page This new procedure involved the removal of the engine and pylon assembly as a single unit rather than as individual components. United's implementation involved the use of an overhead crane to support the engine/pylon assembly during removal and reinstallation. The method chosen by American and Continental relied on supporting the engine/pylon assembly with a large forklift.<ref name="NTSB AAR-79-17 Final Report" />Template:Reference page
If the forklift had been positioned incorrectly, the engine/pylon assembly would not be stable as it was being handled, causing it to rock like a seesaw and jam the pylon against the wing's attachment points. Forklift operators were guided only by hand and voice signals, as they could not directly see the junction between the pylon and the wing. Positioning had to be extremely accurate, or structural damage could result. Compounding the problem, maintenance work on N110AA did not go smoothly. The mechanics started disconnecting the engine and pylon as a single unit, but a shift change occurred halfway through the job. During this interval, even though the forklift remained stationary, the forks supporting the entire weight of the engine and pylon moved downward slightly due to a normal loss of hydraulic pressure associated with the forklift engine being turned off; this caused a misalignment between the engine/pylon and wing. When work was resumed, the pylon was jammed on the wing, and the forklift had to be re-positioned. Whether damage to the mount was caused by the initial downward movement of the engine/pylon structure or by the realignment attempt is unclear.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page Regardless of how it happened, the resulting damage, although insufficient to cause an immediate failure, eventually developed into fatigue cracking, worsening with each takeoff and landing cycle during the eight weeks that followed. When the attachment finally failed, the engine and its pylon broke away from the wing. The structure surrounding the forward pylon mount also failed from the resulting stresses.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
Inspection of the DC-10 fleets of the three airlines revealed that while United's hoist approach seemed harmless, several DC-10s at both American and Continental already had fatigue cracking and bending damage to their pylon mounts caused by similar maintenance procedures.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page The field service representative from McDonnell-Douglas stated the company would "not encourage this procedure due to the element of risk" and had so advised American Airlines. McDonnell-Douglas, however, "does not have the authority to either approve or disapprove the maintenance procedures of its customers."<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
Inadequate speed
The NTSB determined that the loss of one engine and the asymmetrical drag caused by damage to the wing's leading edge should not have been enough to cause the pilots to lose control of their aircraft; the aircraft should have been capable of returning to the airport using its remaining two engines.<ref name=aeat/><ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page The NTSB thus examined the effects that the engine's separation would have on the aircraft's flight control, hydraulic, electrical, and instrumentation systems. Unlike other aircraft designs, the DC-10 was not equipped with a separate mechanism that would lock the extended leading-edge slats into place, relying instead solely on the hydraulic pressure within the system.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page The NTSB determined that the engine tore through hydraulic lines as it separated from the DC-10's wing, causing a loss of hydraulic pressure; airflow over the wings forced the left wing slats to retract, which caused a stall over the left wing.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page In response to the accident, slat relief valves were mandated to prevent slat retraction in case of hydraulic line damage.<ref name="AD80-03-03">Template:Cite web</ref>
The wreckage was too severely fragmented to determine the exact position of the rudders, elevators, flaps, and slats before impact. An examination of eyewitness photographs showed only that the right wing slats were fully extended as the crew tried unsuccessfully to correct their steep roll. The position of the left wing slats could not be determined from the blurry color photographs, so they were sent to a laboratory in Palo Alto, California, for digital analysis, a process that pushed the limits of 1970s technology and necessitated large, complicated, and expensive equipment. The photographs were reduced to black-and-white, which made distinguishing the slats from the wing itself possible, thus proving that they were retracted. In addition, the aircraft's tail section was verified to be undamaged, and the landing gear was down.<ref name=vatz />Template:Reference page
Wind-tunnel and flight-simulator tests were conducted to help understand the aircraft's trajectory after the engine detached and the left wing slats retracted. Those tests established that the damage to the wing's leading edge and retraction of the slats increased the stall speed of the left wing from Template:Convert to Template:Convert.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page The DC-10 incorporates two warning devices that might have alerted the pilots to the impending stall: the slat disagreement warning light, which should have illuminated after the uncommanded retraction of the slats, and the stick shaker on the captain's control column, which activates close to the stall speed. Both of these warning devices were powered by an electric generator driven by the number-one engine, and both became inoperable after the loss of that engine.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page The first officer's control column was not equipped with a stick shaker; McDonnell Douglas offered the device as an option for the first officer, but American Airlines chose not to have it installed on its DC-10 fleet. Stick shakers for both pilots became mandatory in response to this accident.<ref name="ad80-03-10">Template:Cite web</ref>
As the aircraft had reached V1, the crew was committed to takeoff, so they followed standard procedures for an engine-out situation. This procedure is to climb at the takeoff safety airspeed (V2) and attitude (angle), as directed by the flight director. The partial electrical power failure, produced by the separation of the left engine, meant that neither the stall warning nor the slat retraction indicator was operative. Therefore, the crew did not know that the slats on the left wing were retracting. This retraction significantly raised the stall speed of the left wing. Thus, flying at the takeoff safety airspeed caused the left wing to stall while the right wing was still producing lift, so the aircraft banked sharply and uncontrollably to the left. Simulator recreations after the accident determined that "had the pilot maintained excess airspeed the accident may not have occurred."<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page
Probable cause
The findings of the investigation by the NTSB were released on December 21, 1979: Template:Blockquote
Legacy of the DC-10
The crash of Flight 191 brought strong criticism from the media regarding the DC-10's safety and design.<ref name=perception>Template:Cite journal</ref> The DC-10 had been involved in two accidents related to the design of its cargo doors, American Airlines Flight 96 (1972) and Turkish Airlines Flight 981 (1974). The separation of engine one from its mount, the publication of the dramatic images of the airplane missing its engine seconds before the crash, and a second photo of the fireball resulting from the impact, raised widespread concerns about the safety of the DC-10.<ref name=perception/> Another blow to the airplane's reputation was dealt two weeks after the crash when the Federal Aviation Administration (FAA) grounded the aircraft. Although the aircraft itself was later exonerated, the damage in the public's eye was already done.<ref name="DC-10 retirement">Template:Cite news</ref>
The investigation also revealed other DC-10s with damage caused by the same faulty maintenance procedure. The faulty procedure was banned, and the aircraft type went on to have a long career as a passenger and cargo aircraft. In response to this accident, American Airlines was fined $500,000 (equivalent to $Template:Inflation million in Template:Inflation-year) by the US government for improper maintenance procedures.<ref name=aeat/> Earl Russell Marshall, a crew chief at the American Airlines maintenance facility in Tulsa where the last maintenance procedure on the aircraft had taken place, died by suicide the night before he was to be deposed by McDonnell Douglas attorneys.<ref name="The wife of an airline mechanic who committed suicide...">Template:Cite news</ref><ref>Template:Cite book</ref><ref name="Aftermath of DC-10 crash still impacts industry">Template:Cite news</ref>

On June 6, 1979, two weeks after the accident, the FAA suspended the type certificate for the DC-10, thereby grounding all DC-10s under its jurisdiction.<ref name=ad/><ref name=grdunp>Template:Cite news</ref> It also enacted a special air regulation banning the DC-10 from US airspace, which prevented foreign DC-10s not under the jurisdiction of the FAA from flying within the country.<ref name="NTSB AAR-79-17 Final Report"/>Template:Reference page This was done while the FAA investigated whether the airplane's engine mounting and pylon design met relevant requirements. Once the FAA was satisfied that maintenance issues were primarily at fault and not the actual design of the aircraft, the type certificate was restored on July 13, and the special air regulation was repealed.<ref name=faallow>Template:Cite news</ref><ref name="ad">Template:Cite journal</ref><ref name="Aviation Safety">Template:Cite web</ref> The type certificate was amended, however, stating, "removal of the engine and pylon as a unit will immediately render the aircraft unairworthy."<ref name="NTSB AAR-79-17 Final Report" />Template:Reference page
In the wake of the grounding, the FAA convened a safety panel under the auspices of the National Academy of Sciences to evaluate the design of the DC-10 and the US regulatory system in general. The panel's report, published in June 1980, found "critical deficiencies in the way the government certifies the safety of American-built airliners", focusing on a shortage of FAA expertise during the certification process and a corresponding overreliance on McDonnell Douglas to ensure that the design was safe. Writing for The Air Current, aviation journalist Jon Ostrower likens the panel's conclusions to those of a later commission convened after the 2019 grounding of the Boeing 737 MAX. Ostrower faults both manufacturers for focusing on the letter of the law regarding regulatory standards, taking a design approach that addresses how the pilots could address single-system failures without adequately considering scenarios in which multiple simultaneous malfunctions of different systems could occur.<ref name=progress2019>Template:Cite web</ref>
On October 31, 1979, a DC-10 flying as Western Airlines Flight 2605 crashed in Mexico City after a red-eye flight from Los Angeles. The Western crash, however, was due to low visibility and an attempt to land on a closed runway,<ref name=camc>Template:Cite news</ref><ref name=wdcim>Template:Cite news</ref><ref>Template:Cite web</ref> through, reportedly, confusion of its crew.<ref>Template:Cite news</ref>
The loss of Air New Zealand Flight 901 on November 28, 1979, which killed 257 people, added to the DC-10's negative reputation.<ref name=perception/> The Antarctic sightseeing flight hit a volcano,<ref name=upippajc>Template:Cite news</ref><ref name=tfsdic>Template:Cite news</ref><ref name=plblm>Template:Cite news</ref> though this was caused by several human and environmental factors not related to the airworthiness of the DC-10, and the aircraft was later completely exonerated.<ref>Template:Cite web</ref>
Another DC-10 crash 10 years later, United Airlines Flight 232, restored some of the aircraft's reputation. Despite the aircraft losing an engine and all flight controls and crash-landing in a huge fireball (which was caught on video by a local news crew) that killed 112 people, 184 people survived the accident. Experts praised the DC-10's sturdy construction as partly responsible for the high number of survivors.<ref name="DC-10 retirement"/>
Orders for DC-10s dropped off sharply after the events of 1979 (the US economic recession of 1979–82 was also a contributing factor in reduced demand for airliners). From there until the end of production 10 years later, the two largest DC-10 customers were FedEx and the US Air Force (KC-10 Extender). Despite initial safety concerns, DC-10 aircraft continued to serve with passenger airlines for over three decades after the crash of Flight 191.<ref name="DC-10 Final Passenger Flight">Template:Cite web</ref> DC-10 production ended in 1988,<ref name="DC-10 retirement"/> and many retired passenger DC-10s have since been converted to all-cargo use. A DC-10 derivative, the MD-11, constitutes part of the FedEx Express fleet as of June 2025. The DC-10s have been upgraded with the glass cockpit from the MD-11, thereby turning them into MD-10s.<ref>Template:Cite web</ref> American Airlines retired its last DC-10s in 2000 after 29 years of service. In February 2014, Biman Bangladesh Airlines operated the final DC-10 passenger flights.Template:Citation needed
Depictions in media
The National Geographic channel produced a documentary on the crash,<ref name="histch">Template:Cite video</ref> and an episode from Seconds From Disaster titled "Chicago Plane Crash"<ref>Template:Cite episode</ref> detailed the crash and included film of the investigation press conferences. The Canadian television series Mayday profiled the crash in the episode "Catastrophe at O'Hare", which subsequently aired in the US on the Smithsonian Channel and National Geographic Channel's television series Air Disasters.<ref>Template:Cite web</ref> The accident was also discussed in "Breaking Point", the second episode of the first season of TV show Why Planes Crash on MSNBC.<ref>Template:Cite episode</ref>
Chicago folk singer Steve Goodman wrote the song "Ballad of Flight 191 (They Know Everything About It)" in response to the crash and the subsequent investigation as the inaugural song for a series of topical songs that aired on National Public Radio in 1979.<ref>Template:Cite book</ref>
See also
- List of disasters in the United States by death toll
- List of aircraft accidents and incidents by number of ground fatalities
- Aviation accidents and incidents
- Aviation safety
- Similar accidents caused by engine separation:
- Flight 191 - a list of other accident or incident flights with the same or similar number
Notes
References
Further reading
External links
Template:Spoken Wikipedia Template:Commons category
- Memorial in Lake Park, Des Plaines Template:Webarchive
- NTSB Accident Report
- "Public Lessons Learned from Accidents – American Airlines Flight 191" (Archive)
- PlaneCrashInfo.Com – American Airlines Flight 191
- Flight 191 Remembered (Fox Chicago website) (Archive)
- Pre-crash pictures from Airliners.net
- NTSB Probable Cause Report (Alternate, Archive)
- News reports Template:Webarchive at The Museum of Classic Chicago Television
- Template:YouTube
Template:American Airlines Template:Aviation accidents and incidents in 1979 Template:Aviation accidents and incidents in the United States in the 1970s Template:Portal bar Template:Authority control
- Pages with broken file links
- Airliner accidents and incidents in Illinois
- Airliner accidents and incidents caused by in-flight structural failure
- Aviation accidents and incidents in the United States in 1979
- 1979 in Chicago
- 1979 in Illinois
- Airliner accidents and incidents caused by maintenance errors
- American Airlines accidents and incidents
- Accidents and incidents involving the McDonnell Douglas DC-10
- O'Hare International Airport
- May 1979 in the United States
- Airliner accidents and incidents involving in-flight engine separations
- Aviation accidents and incidents caused by loss of control